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So how critical is the diameter of the copper tubing used for the coil. 1/8in = 3.2mm.
1/8 tubing
https://www.ebay.com/itm/Mueller-In...869222?hash=item1eddb86966:g:Uv8AAOSw5T9axVBz
$30
3mm tubing
https://www.amazon.com/dp/B01AN7B46S/?tag=accuratescom-20
$8
A few more - - -Ditto
The last pics - - - -Ditto
Thank you. It was all the info from this thread. Again, thank you.WOW.. you did some really neat design work on your build. Love the bell crank, and the way you lower and raise the trap door. May be it's me but I could not see the 48 volt power supply in your case. That's always been a factor in getting the case smaller. Using the original 1/4" coil for the radiator... interesting !! What are you using to blow in it, to remove heat ? And how effective will it be for continues annealing ?
Looks like the 3mm tubing worked out well for making the coil. Any kinks in winding it ?
Very nice....
Gina
Ma'am, I almost finished. Just waiting for paint to dry on case sides, and to finish leak testing. Some of my notes:
I used almost all of your listed components (Thank you for it).
Case interior is 8"Hx8"Wx12"D. Made from wood, fake wood flooring, and pieces of a video recorder case.
Card is hung and isolated from all vibration.
Fans are mounted to case side. One blowing in, one out at the rad.
There's an air deflector to get the oversized fan to the card's bottom sinks.
I used the 1/4" tube coil that came with the card for a radiator for now.
Shelf is 1"x3"Wx4.5"D UHMW. I had a scrap and will try it for melt.
Solenoid is a scrap 24v, but it works fine.
The LED anneal lamp is blindingly bright, but it lights the brass great.
There was a persistent leak at the pump output nipple even with 2 clamps. Found a parting seam ridge, removed it and all is well - I hope.
I used spade terminal strips as they are more compact.
Here are pics. I'll add more replies.
Only found 5 damaged brass to test with. Running them, the heat coil got hot - then cooled, while the cooler coil kinda almost sorta warmed - then cooled off quick. Flow is quite small. I left a bubble in the vinyl line to watch current. Figuered the copper surface and water volume of the cooler coil was a few times that of the heater.Was wondering how well your home made radiator worked? I have a flow meter in my system and the flow through a 1/8" induction tube is very low (I'm not sure at this low rate how accurate the reading is but I receive pulses and fault the unit out if I don't receive 4 pulses within a second), I'm using a radiator but I'm trying to simplify the entire cooling system. If I just used 1/4" copper tubing for the radiator then I could simplify things but it is a pain to bend without kinking it and using more 1/8 tubing might restrict the flow even more.
Thank you. After many tries on 5 damaged RP brass, .323 Mauser, my start point of tuning is:WOW... Again. My hat is truly off to you. What a neat build, and a lot of ingenuity went into it.
$245.00 went into it, for a precision controlled induction annealing machine. No way you can beat that.
Well done !!
Gina