Here are a couple of photos of my setup. I have never posted these since I personally know that it was not a great installation and did not want to recommend it. Basically the problem is I do not have a mill to precisely/accurately enlarge the holes just large enough to fit both the tube and the bearing. I instead use a drill press. The problem with this is despite my best attempt to immobilize the trickler (which as you know has that odd shape), as the drill bit went through, there was enough torque to move the trickler and make the resultant hole lopsided and too big.
You can see the too big hole in this first photo, I basically filled it in with epoxy which also serve to immobilize the bearing against the trickler body. The nature of these sleeve bearing can be seen in the second photo together with its sloppy side fit.
The good side is despite my poor fitting job, it works perfectly.


You can see the too big hole in this first photo, I basically filled it in with epoxy which also serve to immobilize the bearing against the trickler body. The nature of these sleeve bearing can be seen in the second photo together with its sloppy side fit.
The good side is despite my poor fitting job, it works perfectly.

