Just out of curiosity and I didn't see it mentioned...what was load and how far into the lands or off them were they seated?
Just waiting to see what the borescope shows about the carbon fouling. Thanks for the blow by blow. I think Brownells makes some type of device for extracting separated headless brass. I have had some success with oversize bronze bore brushes. I don't know why a carbide drill bit was used to extract the soft brass stuck case. Sorry about missing the part where you measured neck dimensions. Damaging the chamber with that carbide drill would void any further chamber analysis. I take it that the headspace was excessive due to turning the carbide drill into stuck case and chamber - that must have been close to a 5/8 inch diameter drill.
The brass manufacturer has inspected the cases and my gunsmith has the barrel but hasn’t looked at it yet. Here is what I’ve got so far:
There is nothing in the characteristics of the brass that would be considered defective. The hardness is correct and the wall thicknesses are also within parameters. There is one ruptured case and one intact case. I am told the intact case is barely intact and that it was likely also over pressure. The larger flash hole is most likely due to the brass being deformed when it ruptured. The case head is actually bulged inward from gas venting around the primer and against the bolt face. This forced the primer pocket forward. The case body measurements are all normal for cases fired in a properly sized chamber. The case necks, however, show some possible issues. The case mouths measure .268 for the intact case and .272 for the ruptured case. The neck diameter also increases to .274 as it is measured toward the shoulder. Based on these measurements, it seems the case mouth was somehow constricted causing a drastic pressure increase in the cases.
Now for the barrel:
The barrel was a previously used 6xc cut with an older (smaller) reamer. The neck of the chamber was reamed with a .276 neck reamer for more reliable feeding. The barrel was then used to fire at least 2000 trouble free rounds. I needed a test barrel, so I had the chamber re-cut with a larger 6xcII reamer. This pushed the shoulder about .002-.003 forward. Headspace difference with the new chamber and new brass is .007-.010. It’s more than most would like, but not outside of SAMMI allowances.
The chamber has not been inspected with a borescope yet, but here is what I think may have caused the issue:
The brass previously fired in the old chamber was trimmed each firing to ensure a uniform length and chamfer. The trim length was set once and not changed. There could have been a small amount of carbon buildup in the freebore just forward of the case mouth, but not enough to cause problems. When the shoulder was cut slightly deeper, it allowed the case mouth of the new, untrimmed and longer brass to be pushed into the tight area of carbon buildup. This would cause a huge spike in pressure when fired.
Tubb 2000 Rifle?
When you add a Sako Extractor to a Remington 700 style bolt, you TOTALLY negate the safety enginering placed into the design by Remington. Jackie Schmidt.
Sako Extractor and Coned bolt. Nope. not for me, I had the exact same thing happen to me in a 6BR in a Tubb 2000. Got rid of that death trap quick.
The coned bolt of the Tubb is a known problem only with the 6BR cartridge. It’s NOT a problem with the rifle design. The 6BR has a thinner web and the case head must be 100% supported in any rifle design. If it’s machined properly it’s not a problem at all. I know several shooters that have fired thousands of trouble free rounds of 6BR in their Tubb rifles.
into a carbon ring.
The case mouths measure .268 for the intact case and .272 for the ruptured case. The neck diameter also increases to .274 as it is measured toward the shoulder. Based on these measurements, it seems the case mouth was somehow constricted causing a drastic pressure increase in the cases.
The neck of the chamber was reamed with a .276 neck reamer for more reliable feeding.
I had the chamber re-cut with a larger 6xcII reamer. This pushed the shoulder about .002-.003 forward. Headspace difference with the new chamber and new brass is .007-.010. It’s more than most would like, but not outside of SAMMI allowances.
When the shoulder was cut slightly deeper, it allowed the case mouth of the new, untrimmed and longer brass to be pushed into the tight area of carbon buildup. This would cause a huge spike in pressure when fired.
Probably excessive headspace was the cause.
I say this because you didn't measure the base to datum of all the new brass, so you really don't know if it was all within spec.
Seems the neck got pinched in the small or short chamber.
That’s my best guess as well. Unfortunately, there were no obvious problems visible in the chamber.