AlNyhus
Silver $$ Contributor
Here's another way to deal with the 'lump' after expanding 6BR cases to .30.
A Redding 7BR Body Die has a .311 opening for the neck. So I took one of those:
Added an 'o' ring under the lock ring and screwed it into my 'stub' threaded 7/8-14. The 'o' rings allows for a bit of self centering.
With the stub and die in the chuck, it was time for this. It's a stepped carbide chucking reamer that's .311-.327. The .311 registers in the hole through the die and the .327 section cuts the neck portion to .327.
After opening up with the reamer:
The internal finish of the new neck is pretty nice as verified by bore scoping. I did a light bevel on the inside of the die at the neck/shoulder junction with a 30 degree tapered stone:
This is a Lapua 6BR case expanded to .30. Checking the run out, it's right at .0045...pretty normal after mechanically expanding the neck.
After running the case through our new fixed neck dimension die, here's what we get. You can see the 'lump' has been reduced in external dimension:. Leaving the 'o' ring under the lock ring allows some float and lets you adjust the die down until you've gone past the 'lump'. With a pin gage, there's no more tightness at the neck/shoulder junction than before going through the die:
Run out after going through the die:
Then I just went over a .3070 expander and turned the case on a .3060 carbide mandrel like normal. Post turning, the neck shows minimal run out:
I ran the cutter down the shoulder a bit more than normal to show how even the cut was at 180 degree intervals. Excessive neck run out would show the wavy cut you get when there's excessive neck runout prior to turning.
Hope some will find this helpful.
-Al
A Redding 7BR Body Die has a .311 opening for the neck. So I took one of those:

Added an 'o' ring under the lock ring and screwed it into my 'stub' threaded 7/8-14. The 'o' rings allows for a bit of self centering.


With the stub and die in the chuck, it was time for this. It's a stepped carbide chucking reamer that's .311-.327. The .311 registers in the hole through the die and the .327 section cuts the neck portion to .327.


After opening up with the reamer:

The internal finish of the new neck is pretty nice as verified by bore scoping. I did a light bevel on the inside of the die at the neck/shoulder junction with a 30 degree tapered stone:

This is a Lapua 6BR case expanded to .30. Checking the run out, it's right at .0045...pretty normal after mechanically expanding the neck.

After running the case through our new fixed neck dimension die, here's what we get. You can see the 'lump' has been reduced in external dimension:. Leaving the 'o' ring under the lock ring allows some float and lets you adjust the die down until you've gone past the 'lump'. With a pin gage, there's no more tightness at the neck/shoulder junction than before going through the die:

Run out after going through the die:

Then I just went over a .3070 expander and turned the case on a .3060 carbide mandrel like normal. Post turning, the neck shows minimal run out:

I ran the cutter down the shoulder a bit more than normal to show how even the cut was at 180 degree intervals. Excessive neck run out would show the wavy cut you get when there's excessive neck runout prior to turning.


Hope some will find this helpful.

Last edited: